mx6cuboxi: failes to detect model
Fabio Estevam
festevam at gmail.com
Tue Mar 26 19:08:00 CET 2024
On Tue, Mar 26, 2024 at 1:11 PM Christian Gmeiner
<christian.gmeiner at gmail.com> wrote:
> It got better but the model is (still) wrong:
>
> U-Boot 2024.04-rc5-dirty (Mar 26 2024 - 17:03:41 +0100)
>
> CPU: Freescale i.MX6Q rev1.3 996 MHz (running at 792 MHz)
> CPU: Extended Commercial temperature grade (-20C to 105C) at 20C
> Reset cause: POR
> Model: SolidRun HummingBoard2 Dual/Quad (1.5som+emmc)
> Board: MX6 HummingBoard2
> DRAM: 2 GiB
> Core: 82 devices, 17 uclasses, devicetree: fit
> MMC: FSL_SDHC: 1, FSL_SDHC: 2
> Loading Environment from MMC... *** Warning - bad CRC, using default environment
It seems to me that there is a mix of DM GPIO and non-DM GPIO.
Does the change below help?
--- a/board/solidrun/mx6cuboxi/mx6cuboxi.c
+++ b/board/solidrun/mx6cuboxi/mx6cuboxi.c
@@ -336,20 +336,16 @@ static enum board_type board_type(void)
* HB 1 1 x
*/
- gpio_direction_input(IMX_GPIO_NR(2, 8));
- val3 = gpio_get_value(IMX_GPIO_NR(2, 8));
+ val3 = !!dm_gpio_get_value(&(board_detect_desc[0]));
if (val3 == 0)
return HUMMINGBOARD2;
- gpio_direction_input(IMX_GPIO_NR(3, 4));
- val2 = gpio_get_value(IMX_GPIO_NR(3, 4));
+ val2 = !!dm_gpio_get_value(&(board_detect_desc[1]));
if (val2 == 0)
return HUMMINGBOARD;
-
- gpio_direction_input(IMX_GPIO_NR(4, 9));
- val1 = gpio_get_value(IMX_GPIO_NR(4, 9));
+ val1 = !!dm_gpio_get_value(&(board_detect_desc[2]));
if (val1 == 0) {
return CUBOXI;
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